EASIIR aciliry- Wide Report FACILITYID mr 3" F4 IMME i it 1 is 1 - "elf ge, fgawt rm it a S114 TUS 5; Fo x;t gf;i5~ in -u -L. ., gf g;r_ ADDRESS me .ss a 411 Puff . . ..fe shCITY 5 HP CODE . . -ii, . - "f?5E i . ==lxilIrs'grew :gigs #ge as inf'rw vest <*nr fat, c, 'Eg *feEgff tau* Becky Macionskl anon LEVIITS PM VE STDs. lil ILNREGULA TED EUS El EVSIGNIEICANT EUS El Voc os sms. OTHER FAC. REQS. EAC: CUMPL. STA AS on ACTIVITY CODE: OTHER Compliance inspection conducted by myself and James Burkholder along with auditing metals, HCI and COBMENTS PM testing on Boiler 3. Prior to observing stack tests, James and I went with Becky Macionski to the control room to observe operating rates and CEMS pollultant values. Boiler 2 is currently clown for repairs described in 007 AC permit Borler1 and Boller 3 were both operating. Becky provided a 4-hour average report for 4/27 The following values were observed for Boiler 1 in the 0400 0800 4~hour block CO 190 SDA outlet temp 314 4 F, steam rate' 226 200 ib/hr. For Boiler 3 34 SDA outlet temp: 324.8 F, steam rate 234 600 Ib/hr The CO excess emissions for Bo1ler1 was attributed to a feed chute plug that occurred in the morning. Hourly data was observed for Nox and S02 On Boiler 1 there was a max. Nox value of 225 at 0900 There was a max. S02 value of 119.6 at 0600 (29% reduction) On Boller 2 there was a max. Nox value of 21 8.5 at 0300 There was a max S02 value of 55 On Boiler 1, mln. observed carbon feed rate was 17 62 at 0600 On Boller 3 min. observed feed rate was 14.52 at 0900. Due to upcoming DF testing, no apply to MWC unit load or fabric filter temperature. Test audit data is being prepared on a separate report by James Burkholder. (69% reduction) at 0700. Carbon feed rate records were observed for hours 0000-0900 on Boiler1 and 3. INSPECTORS: itil* Max Grondahl SWD max.grondahl@clep.state.fl.us 813/632-7600 ext James Burkholder SWD DVSPECTION DA TE INSPECTION STATUS 27, 2009 See Reports for more details Pinell County Resource Recov Pinellas County, Florida Average Report - (60-min) Report for 4/27/2009 12:00:00 ANI to 4/27/2009 Facility 11:59:59 PM Device: Interval: 1-hour average Name SO2 Corr Corr SO2 RE Corr Corr S02 Corr Corr S02 RE 00:00 175.6 33.0 64.35 0.1 6.5 189.3 30.7 82.91 01:00 188.3 68.2 26.64 1.0 6.5 202.7 21.8 88.24 02:00 196.9 43.9 64.13 0.1 6.6 213.0 20.4 88.26 03:00 202.6 106.2 0.26 0.0 6.7 218.5 39.3 84.74 04:00 203.3 50.9 35.43 0.0 6.8 197.2 22.2 89.35 05:00 181.1 53.2 51.58 1.2 '6.8 167.1 30.8 84.78 06:00 171.6 119.6 28.93 0.0 6.6 162.1 33.7 78.06 07:00 194.2 56.8 39.03 23.6 2.7 174.8 55.0 69.25 08:00 201.1 8.9 85.90 0.0 5.6 177.8 12.8 78.07 09:00 225.0 6.8 87.75 1.5 5.9 176.4 13.0 63.82 10:00 11:00 12:00 13:00 14:00 15:00 16:00 17:00 18:00 19:00 20:00 21:00 22:00 Max 225.0 119.6 870% 218.5 55.0 89.35 Min 171.6 6.8 0.26 162.1 12.8 63.82 Avg i 194.0 54.7 48.40 187.9 28.0 80.75 #Valid invalid User Data - Calibration - Process Down - Maintenance - Error - Out-of-Control - Not Calibrated - Excess Emission - Caution - Frozen FIFO Time zone: Eastem Daylight Time Report printed on Monday, April 27, 2009 10:25:00 AM Page 1 of 1 Pinel County Resource Recov Facility Pinellas County, Florida Average Report - (4-hour) Report for 4/27/2009 12:00:00 ANI to 4/27/2009 11:59:59 PIVI Device: Interval 4 hour average Name B1 ln O2 B1 SDA Steam B3 In O2 B3 SDA B3 Steam Corr CO Out Temp Rate Corr CO Out Temp Rate Pl'-lm 00:00 92 320.7 230.6 54 319.8 230.8 04:00 190 314.4 226.2 34 324.8 234.6 08:00 12;00 C7049 16:00 - -..-- Max I 190 320.7 "zsof?" 54 324.8 234.6 92 314.4 226.2 34 319.8 230.8 Avg 141 317.6 228.4 44 322.3 232.7 #Valid Invalid - User Data - Calibration Process Down Nl - Maintenance - Error - Out-of-Control Not Calibrated - Excess Emission - Caution - Frozen FIFO Time zone: Eastem Daylight Time Report printed on Monday, April 27, 2009 10 22 All/I Page 1 of 1 Pinel County Resource Recov Facility Pinellas County, Florida Average Report - (60~min) Report for 4/27/2009 12:00:00 AM to 4/27/2009 11:59:59 PM Device: interval: 1-hour average Name B1 Feed B3 Feed Rate Rate DPU 00:00 17.91 17.63 01:00 17.92 17.84 02:00 17.73 17.73 03:00 17.93 17.86 04:00 17.82 17.59 05:00 17.71 17.62 06:00 17.62 17.96 07:00 17.94 16.04 08:00 17.79 15.01 09:00 17.72 14.52 10:00 11:00 12:00 13:00 14:00 15:00 16:00 17:00 18:00 19:00 20:00 21:00 22:00 Max i 17.94 17.96 Min 17.62 14.52 Avg i 17.81 16.98 #Valid I 10 10 I - Invalid - User Data - Calibration - Process Down - Maintenance - Error - Out-of-Control - Not Calibrated - Excess Emission - Caution - Frozen FIFO Time zone: Eastern Daylight Time Report printed on Monday, April 27, 2009 10:22:07 AM Page 1 of 1 5 1 '91 ISOKINETIC FACILITY: I _f TEST |_ocAT|oN: TE: aa PM IPOLLUTANT: RuN|.n.= [go I DG DGM TEMP TEMP EXI FILTER METER INLET OUTLET TEMP TEMP VAC 5 [Tl bo 2112? II FIIEI RUN STACK STACK METER DGM VOLUME POINT NIE TIME STATIC TEMP ll-ilH%fl! 1 1. 5 Ill!-I 515 0 555 1 sz, EilWLTI- 0 2, 3 KEITH T3 EHIZHII '7'7 oi5 -I 3% EEKIIHFHEIEQII 3% -15525 5717 IFZEIIQK QsIHETEHYHIEI -EEIEKI 52 Ei'l1ff? ZS lil ww -P211 $25135 1 fo' 625% EUR 196' El "Il 5 S7 EHIKTI 3: 2, HI --BTI TW Hillifl -IEWI 57 IHI-T.. Illfil Z?1l? (C) 87 7, a. I iil FQFZ LEAK CHECK. PITOT 7% OF cusToDY VACUUM 5" PRE CONTAINER SAMPLE 1 DESCRIPTION RATE 09 $0 POST IMPINGER CONTENTS INITIAL FINAL -- NOZZLEKIJ BOXID I wsu "'Ii"7 PROBE ID 4 5. I yn.-5 . . TI AP AH F`frOr wr VPAGE EQFL FACILITY: TESTOQTION: ggi' 9 I 5 055g -M -R 1 DGM DGM STACK STACK METER VOLUME DGM IN EXIT FILTER POINT TIME TIME STATIC TEMP. AP AH fla TEMP. TEMP. TEMP TEMP. VAC. I I 1" PAGE _jor=_L I i TEST LOCATION: TE: TECHNICIAN PEAR POLLUTANT: RUN -M I POINT TIME TIIVIE STATIC TEMP. AP AH F`t3 INLET OUTLET TEMP TEMP. VAC111-1 CHAIN OF CUSTODY1 LEAK CHECK: PITOT 7 I IMPINGERCOWENTSI 1si,